FINAL TECHNICAL REPORT
November 1, 1998, through January 31, 2000
Project Title:SCALE UP OF THE ISGS FROTH WASHER FOR TESTING IN A COMMERCIAL PLANT
ICCI Project Number: 98-1/4.1A-1
Principal Investigator: L. A Khan, ISGS
Other Investigators: J. Lytle, W. Roy, Y. Simpson, H. Massood and D. Patil ISGS
Project Manager: Ken Ho, ICCI
ABSTRACT
The purpose of this project was to scale up the ISGS froth washer for testing at a commercial plant. Specifically, the approach taken was to scale up the ISGS washer by more than a factor of ten from a 0.11-ft3 miniature cell to a 1.3-ft3 cell. The washer has been developed at the ISGS to increase the throughput and cleaning efficiency of a froth flotation circuit.
Our goal for this phase has been to determine
the shape and dimensions of the ISGS washer, which from its proof-of- concept
to pilot-plant scale has been developed in two years, and is capable of
processing effectively the concentrate generated in a plant. To accomplish
this goal, a versatile washer was designed first. A rectangular-shaped washer
that increases the cross-sectional area, but maintains a shallow froth to
maintain a high rate of rejection of fine pyrite and clay particles was selected.
Also, to limit the contact of the stream of contaminants with the
stream of froth, grooves were added to the bottom of the washer to enhance
the flow of the streams of contaminants thereby minimizing the contact of
the froth with the streams of contaminants
This washer was then tested on a miniature cell to determine optimum operating conditions. To achieve this goal, tests were conducted first to determine important operating parameters and their effective sphere of influence. Using a statistically designed matrix of experiments the impact of the simultaneous change, within certain limits, of these important parameters on the performance of the washer and hence, the optimum operating conditions were determined. It was able to produce under certain conditions a cleaner product with less sulfur than that predicted by the Advanced Flotation Washability Analysis Curve (AFWAC).
The next task was to determine whether a pilot-plant
cell equipped with the washer will perform as well as the miniature cell
washer. Tests on the 1.3-ft3 subaeration cell equipped with the
washer were carried out. Even at one third of its capacity the larger washer
handled, irrespective of the ash content of the feed, all the froth that
was generated in this cell and produced a product that was often better than
that predicted by the AFWAC. An increase in its size improved the stability
of the cell. The larger cell was even more stable than its miniature version
and operating smoothly.
Pages 1-30 contain propriety information and are not available for distribution except to the sponsor(s) of this project.
EXECUTIVE SUMMARY
The circular washer developed at ISGS when attached to a subaeration cell, had produced consistently a product that was cleaner than that produced with a packed column using the same feed material. Also, the rate of production of concentrate of the cell with the washer was greater than that of ordinary flotation columns. The goal of this project was to design a washer that could be used in an industrial environment and help a subaeration flotation cell produce clean coal in single-stage flotation tests. Commercial development and installation of such a device will have a significant impact on the future of the coal industry in Illinois by increasing recovery of fine coal and decreasing coal washing costs.
During the intensive washing and enhanced drainage that occur in the inclined
washer, both the particles that are mechanically carried over, unselectively
attached to the froth and those that are trapped between the air bubbles
are flushed out. To make sure that flushed particles do not become re-entrained
in the lower layers of the froth, it is better to limit the vertical height
of the froth that is being washed. In the ISGS washer, the washed-out minerals
are carried a short vertical distance to a separate stream along the lower
part of the washer, and not allowed to become entrapped again.
Without the usual multiple stages of cleaning and re-cleaning, the ISGS washer
allows a single flotation cell to produce a product cleaner than that produced
by a flotation column at the throughput rate of a common subaeration cell.
In other words, this device is an improvement on the old system of subaeration
cell batteries in which the froth or tails were recleaned to generate a product
of desired quality. Equipped with this device, each cell can produce the
final product in a single run leading to greatly increased capacity of the
plant or a decrease in the number of the cells required to process a given
quantity of material. The result may be considerable savings in installation
and/or operational cost. Costs also will be saved because of the better cleaning
efficiency of fines and because of the associated saving on disposal of fines.
The ISGS washer has been tested on both a subaeration cell and a column.
A froth flotation system retrofitted with the inclined washer produces better
grades and recoveries than the most advanced systems being developed - sometimes
even better grades and recoveries than those predicted by the Advanced Flotation
Washability Analysis Curve (AFWAC). There are several reasons why the ISGS
washer can operate so effectively:
The ISGS washer can be operated successfully to produce a well-drained dry froth or a very wet, water-laden froth depending on the needs of the system and the capacity of the filtration system. In either case, the coal produced is cleaner than that produced by advanced columns.
In the subaeration flotation, aeration rate was used to increase the recovery. Unlike the results from the circular 4-inch inclined washer, it appears that the capacity of the 2-inch circular inclined washer was pushed to its limit as the throughput was increased to 200 lb/hr/ft3. At a smaller throughput however, a much smaller ash content of 5.9% was produced. The most likely reason that the 2-inch ID washer could not be increased to the same throughput capacity as the 4-inch ID washer was because of the velocity of the froth. The faster the froth moves through the washer, the greater the tendency for it to push some of the stream of water trying to carry contaminants down to the bottom of the washer back up instead. However, it appears that increasing the diameter of the washer can have a negative effect on rejection of the fine pyrite particles. Our best pyritic sulfur rejection (0.5% PS) in the earlier version was attained in the 2-inch ID washer at low throughput. The ability to reject fine pyrite particles appears to decrease with increased diameter and increased throughput. One of the most important tasks for scaling up of the ISGS washer for use in a plant was to design its shape and size to overcome that problem. It was felt that a rectangular-shaped washer that increases the cross-sectional area, but maintains a shallow froth to maintain a high rate of rejection of fine pyrite and clay particles, would do the job. It was also felt that grooved-bottom washer would limit the contact of the froth with minimizing the contact of the froth with the streams of returning contaminants through the grooves.
Our goal for this phase has been to determine
if the rectangular washer will work under maximum load, how the capacity
of the washer could be increased if required without increasing its depth,
and how to construct a similar washer for a pilot-plant cell. The performance
of pilot-plant cell was also tested in the laboratory to ensure that its
performance was similar to that of the table top cell and from that data
to design, construct and test a modified plant-size unit if required.
To conserve feed it was felt that a
miniature cell should be used during the tests
required to find the maximum throughput load and optimum operating
condition. A 0.11 ft3 replica
of an industrial subaeration cell was prepared. Then a rectangular
shaped washer of appropriate size was designed, built and attached to this
miniature cell. A rectangular-shaped washer
increases the cross-sectional area, but maintains a shallow froth to maintain
a high rate of rejection of fine pyrite and clay particles. Also, to limit
the contact of the stream of contaminants with the stream of froth, grooves
were added to the bottom of the washer for the streams of contaminants to
flow along, minimizing the contact of the froth with the streams of
contaminants.
Flotation tests were then conducted in the miniature cell attached to the
miniature washer by varying one parameter at a time to determine the important
parameters and their range of influence. Because the change in one variable
at a time does not take into account the interaction of the variable among
themselves and their combined effects on the process, a matrix of tests was
designed statistically that will help determine the optimum operating conditions
of the miniature cell and of the washer. Tests were then carried out according
to this statically designed scheme and optimum operating conditions were
determined. Tests on the miniature cell and
washer were conducted when washer was used only at 1/3 of its capacity.
The impact of variables such as the angle of inclination of the washer, the
amount of wash water, stages of washing/length of washer, aeration rate and
feed rate on the quality and quantity of material produced in flotation machines
equipped with ISGS washer were determined. Under many of these conditions,
the miniature cell and washer gave better results than predicted by the AFWAC.
The overall goal of our proposed work for 1998-1999 has been to scale-up
the ISGS washer for use at a commercial plant. A 1.3-ft3 Denver
subaeration cell (more than a factor of ten larger than the miniature subaeration
cell) was prepared for the pilot-plant tests. Three different washers were
built to ensure that all the concentrate that is produced by the cell is
handled efficiently. Tests were then conducted in the pilot-plant scale
subaeration cell equipped with the ISGS washer of the smallest capacity.
Fine coal , rejects, and a 1:1 mixture of the fine coal and reject from the
same mine were used as a feed in these tests. The preparation plant rejects
contained large amounts of clay-sized minerals, pyrite and a broad particle
size distribution. As such, these fines required a carefully designed inclined
washer. The fine coal on the other hand produced larger amount of concentrate
which would tests the limits of the washer. The results of these tests were
compared with the results of 1.3-ft3
cell. The 1.3-ft3 subaeration
cell did not require more than 1/3 of its smallest washer to clean all of
the froth generated. The operation of the larger cell were more stable than
those of the miniature cell and hence it produced under certain conditions,
a much cleaner product than predicted by the AFWAC.
Its pyritic sulfur rejection was much better
than that predicted by the AFWAC.